04-24-2004, 05:32 PM
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Some blowby #4 low pulled piston and nothing wrong??
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Naturally Aspirated
Join Date: Mar 2004
Location: Boynton Beach, FL
My Ride: 1992 IROC R/T
Engine: 2.2L TIII
Induct: Turbo
1/4: 0.000
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That pretty much says it all. My turbo blew and made a real mess but at the EXACT same time all of a sudden i started getting some blowby out the dipstick tube.
I did a compression check and all pistons were 130-135 except for #4 which was about 115-120. And this is the cylinder that my EGT is tapped for. I know my temps have been fine and pulling the head revealed i was running **** rich too. So i popped the piston out anyways and it looks perfect. I even took off the top two rings and they look fine too.
The only question i have is with the hastings rings i know the dot goes up on the second ring but on the top ring is that beveled edge suppose to go up or down? B/c it was up and on the second ring even though the dot is up the edge is down. Any ideas?
Im kinda at a loss as to what i can do to find out why #4 had low compression. The only option i can see at this point is to buy new rings and rering the whole engine again since nothing is wrong with the piston.
Oh and the pistons i am using is the Ross racing Forged pistons. .020 oversized.
I need help in a bad way as i wanted to have the car ready for Cliffs Mopar Day at Cecil and the Mopar Atlantic Nats.
All help is appreciated! Oh yeah this is an 89 CSX with a common block engine.
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