 |
|
  |
 |
11-01-2004, 07:10 PM
|
#2
|
  |
|
|
|
Naturally Aspirated
Join Date: Feb 2003
Location: Hampton Roads, Virginia
My Ride: 1987 Shelby GLH-S
Engine: 2.2
Induct: Turbo
1/4: 0.000
|
I had the same problem and used two very small washers between the AFPR and the rail and it sealed just fine. I think the Accufab seats too low and prevents a good seal. Just what worked for me!
|
|
|
|
 |
  |
  |
 |
11-01-2004, 07:30 PM
|
#3
|
  |
|
|
|
Naturally Aspirated
Join Date: Jan 2003
Location: www.TurboDodge.com
My Ride: 1986 Plymouth Horizo
Engine: 2.2 Turbo
Induct: Turbo
1/4: 11.705
|
Yup, mine also came with the washers.
|
|
|
|
 |
  |
  |
 |
11-01-2004, 11:52 PM
|
#5
|
  |
|
|
|
Naturally Aspirated
Join Date: Jul 2003
Location: Kansas City
My Ride: 89 Daytona ES
Engine: 2.2L TII
Induct: Turbo
1/4: 0.000
|
Well i don't know what to think now? I got my Accufab from FWD-P, no washers, seats perfect?
|
|
|
|
 |
  |
  |
 |
11-02-2004, 11:40 PM
|
#7
|
  |
|
|
|
Naturally Aspirated
Join Date: Jan 2003
Location: Upland, CA
My Ride: 2000 GMC Sierra
Engine: 5.3L V8
Induct: N/A
1/4: 0.000
|
Got mine from Relentless and I used 2 washers
|
|
|
|
 |
  |
  |
 |
11-03-2004, 07:25 AM
|
#8
|
  |
|
|
|
Naturally Aspirated
Join Date: Jan 2003
Location: Southgate, KY
My Ride: 1987 Shelby GLHS 189
Engine: 2.2L
Induct: Turbo
1/4: 12.510
|
 Quote:
|
Originally Posted by diabloed
Well i don't know what to think now? I got my Accufab from FWD-P, no washers, seats perfect?
|
  |
You are lucky... They usually score the rail.. then they never seal right.
|
|
|
|
 |
  |
  |
 |
11-04-2004, 02:57 PM
|
#10
|
  |
|
|
|
Naturally Aspirated
Join Date: Jul 2004
Location: Terryville, CT.
My Ride: 1986 GLHS #065
Engine: 535hpAluminumLongRod
Induct: Turbo + Nitrous
1/4: 11.921
|
 Quote:
|
Originally Posted by diabloed
Well i don't know what to think now? I got my Accufab from FWD-P, no washers, seats perfect?
|
  |
Same here.
|
|
|
|
 |
  |
  |
 |
11-04-2004, 03:58 PM
|
#11
|
  |
|
|
|
Naturally Aspirated
Join Date: Jan 2003
Location: Southgate, KY
My Ride: 1987 Shelby GLHS 189
Engine: 2.2L
Induct: Turbo
1/4: 12.510
|
A reason for no leaks is quite likely it's been put on (the o-ring slipped in un-fazed) but not taken off yet. The damage happens after tightening. The nut cuts small grooves. When the FPR is mounted the next time, these grooves make small slices in the sealing area of the O-ring. The rest is history... You need to sand the "slices" out to fix it.
Again... if you've had it on and off several times and its still sealing, CONSIDER yourself lucky. Experience is what is being doled out here. Takes 2 seconds to do it right rather than take a chance.
GREAT PIC Chris
|
|
|
|
 |
  |
  |
 |
11-04-2004, 05:07 PM
|
#12
|
  |
|
|
|
Boostaholic
Join Date: Jan 2003
Location: PirateSwashbucklers.awesome
My Ride: 88 Plymouth Reliant
Engine: 2.5L T2
Induct: Turbo
1/4: 0.000
|
yeah mine doesnt have the washers (didnt know when i put it on a while ago) and it still seals fine... however, i never took it off and I dont plan on it unless I get a larger fuel rail or if I make a high flow fuel rail.
BRian
|
|
|
|
 |
  |
  |
 |
11-05-2004, 10:17 PM
|
#13
|
  |
|
|
|
Naturally Aspirated
Join Date: Apr 2003
Location: Lincoln, Ne
My Ride: 91 Spirit R/T
Engine: TIII
Induct: Turbo
1/4: 0.000
|
Hmmm. Yup, I'm a dumbass. I simply used some loctite and left the nuts not totally tightened. Oh well. The GLHS isn't going to get driven anytime in the forseeable future. Washers are going on anyways though. they're what? 10 cents at the hardware store?
|
|
|
|
 |
  |
  |
 |
11-13-2004, 01:56 PM
|
#14
|
  |
|
|
|
Naturally Aspirated
Join Date: Nov 2004
Location: NE Ohio
My Ride: 87 Z
Engine: 2.2 (+.040)
Induct: Turbo
1/4: 14.130
|
Same thing happened on my shelby z. I'm in the process of trying to fix it today. I've already used the spare o-ring I had. Went and got several o-rings (just in case) and will try the washer trick. the rail is somewhat scored though.  I'll let you know how it goes...
|
|
|
|
 |
  |
  |
 |
11-14-2004, 11:14 AM
|
#15
|
  |
|
|
|
Naturally Aspirated
Join Date: Nov 2004
Location: NE Ohio
My Ride: 87 Z
Engine: 2.2 (+.040)
Induct: Turbo
1/4: 14.130
|
Well, I ended up having to pull the whole damn rail out, as I couldn't get anything in there to fix the scoring while installed. What a chore! If it weren't for that damn pulse dampener... Anyway I used a small buffing wheel on the ol' dremmel and polished out the scoring then actually used some petroleum jelly when re-installing everything, and the 60psi bursts aren't blowing it out anymore. I think I got real lucky. BTW I stuck the washers down in the rail between it and the reg. so I could put a little torque on those nuts without the risk of shoving the hex back down in there. Whatever works though...
|
|
|
|
 |
  |
 |
|
|
Currently Active Users Viewing This Thread: 1 (0 members and 1 guests)
|
|
|
Posting Rules
|
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts
HTML code is Off
|
|
|
|
» Quick Nav |
|
» Quick Tech |
|
» Market Place |
|
|
|
|
|
|
|
|
|
|
|